NTSB to determine probable cause of Boeing 737 door plug blowout Tuesday

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"NTSB to Announce Findings on Boeing 737 Door Plug Incident Investigation"

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On January 4, 2024, a significant incident occurred involving a Boeing 737 Max when a door plug blew out at an altitude of over 16,000 feet, resulting in a large hole on the side of the aircraft. The National Transportation Safety Board (NTSB) is set to review the investigation findings on Tuesday, which will include a vote to determine the probable cause of this alarming event. The incident raised serious concerns regarding Boeing's manufacturing practices, particularly after the recent fatal crash of a 787 Dreamliner operated by Air India. Although it remains unclear whether Boeing's actions directly contributed to that crash, the company’s reputation has already been severely compromised following two tragic 737 Max crashes in 2018 and 2019, linked to design flaws and software issues. The pressure mounts as Boeing faces scrutiny, and the NTSB's findings could either alleviate or exacerbate the situation for the manufacturer, which has little credibility left to lose.

The preliminary findings from the NTSB indicated that the door plug was missing four essential bolts at the time of the aircraft's delivery to Alaska Air in October 2023. This oversight occurred despite the plane successfully completing 153 flights over a span of ten weeks, which included several trips between Hawaii and the mainland. The incident could have had catastrophic consequences had it occurred at a higher altitude over the Pacific Ocean. Investigators highlighted that there was no documentation to suggest that the door plug had been removed and improperly reinstalled without the bolts. Workers on the production line were reportedly unaware of the need for these bolts, and testimonies from Boeing employees revealed that there was significant pressure to expedite assembly processes, leading to oversights. In response to this incident, the Federal Aviation Administration has imposed stricter oversight on Boeing and limited its production levels. Boeing has stated that it is taking steps to enhance the quality and safety of its aircraft, including changes in leadership, following the incident. A complete report from the NTSB regarding the Alaska Air incident is expected to be released in the coming weeks.

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On January 4, 2024, a door plug blew out on aBoeing 737 Maxat more than 16,000 feet in the air, leaving a gaping hole in the side. On Tuesday, the National Transportation Safety Board will hear the investigation’s findings and vote on the probable cause of the incident was.

The findings could put to rest one of the biggest questions around the terrifying incident: Who is to blame?

The hearing comes at a fraught time for Boeing, as well, which is now the focus of the fatalcrash of a 787 Dreamliner operated by Air Indiathis month.

While there is no indication yet that Boeing’s work caused the crash of the nearly 11-year-old plane, confidence in Boeing could suffer further unless it is cleared as the cause. And after two fatal 737 Max crashes in 2018 and 2019, respectively, were traced back to design and software errors, and the Alaska Air door plug incident was caused by the jet being delivered to the airline by the embattled aircraft maker without the four bolts needed to hold it in place, Boeing had little reputation left to lose.

In the January 2024 door plug blowout, passengers’ clothing and phones were ripped away and sent hurtling out of the plane, and the missing piece from Alaska Air flight 1282 was later found in an Oregon backyard. Through a combination of crew skill and luck, with no one seated next to the hole, it could easily haveturned into a tragedy.

In the NTSB’s preliminary findings,it was revealed that four bolts that hold the door plug in place on the Boeing 737 Max were missing at the time of the plane’s delivery to Alaska Air in October 2023. The plane made 153 flights over 10 weeks before the incident, including 22 flights between Hawaii and the mainland. Had the incident occurred over the Pacific at 35,000 feet rather than minutes after taking off from Portland airport, it could have led to the loss of the plane.

What has not been revealed is who exactly was responsible for leaving the bolts off the door plug during the manufacturing process. Boeing revealed there wasno internal paperworkshowing that the door plug had been removed and then put back in place without the bolts, so workers who were moving the plane along the production line were not aware it needed to have the bolts reattached.

The NTSB already held afact finding hearinginto the incident in August, where it revealed interviews with Boeing employees who said they felt pressure to work too fast to avoid mistakes.

A Boeing employee, identified as a Door Master Lead, told investigators that much of the assembly work needed to be redone because of the later discovery of problems, as happened with the door plug that was removed to fix some rivets.

The worker said there was no special training to open, close or remove a door plug versus a regular door. The worker’s team was“put in uncharted waters to where… we were replacing doors like we were replacing our underwear.”

As a result of the incident the Federal Aviation Administration announced additional oversight of Boeing and limits on its production levels. The aircraft maker only recently returned to the production level for the 737 Max that it planned ahead of the incident.

Boeing said it has taken its own steps to improve the quality and safety of its planes, and it replaced the CEO at the time of the incident, Dave Calhoun. And last month the Justice Departmentdropped criminal chargesit had planned against Boeing for defrauding the FAA during the certification process for the Max ahead of two fatal crashes in 2018 and 2019.

The complete final report on the Alaska Air incident from the NTSB will be available in a few weeks.

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Source: CNN